基于MES實(shí)時數(shù)據(jù)采集與控制系統(tǒng)的研究與設(shè)計
[Abstract]:With the rapid development of manufacturing informatization and industrial automation, the demand of manufacturing execution system (MES) for manufacturing enterprises is increasing. At present, the function of MES in our country is not perfect, the integration degree is low, the real time effect is not good, the automation control is backward and so on. The MES system built on the integrated network will effectively control the implementation process of the workshop, reduce the waste rate, reduce the material wastage, grasp the production data in real time, and realize the traceability of the data. Provide effective support for the management, operation and planning of the whole enterprise. Firstly, this paper analyzes and studies the two function modules of MES, which are data acquisition and process control in detail, and proposes an integrated real-time data acquisition scheme and an intelligent active control scheme. In the aspect of data acquisition, based on the research results of NC equipment in manufacturing industry, this paper classifies NC equipment into three categories: traditional NC machine tool, customized special machine equipment and advanced NC equipment. The networked data acquisition schemes are designed for three kinds of NC equipments, which provide reference and support for the integrated design of MES. In the aspect of active control, this paper puts forward a solution that takes PLC as the main controller and the production line server participates in the collaborative control. The structure limitation of control layer, execution layer and plan layer is broken, and the control function module between the bottom control system and MES is integrated. Through the interaction of the integrated system of the bottom machine tool and MES-ERP, the autonomous control of the underlying equipment is realized. Then, on the basis of the research of the scheme, this paper designs a MES system for E2 pipe assembly line customized by Zepper steering system Co., Ltd. In the aspect of data acquisition, the local PLC module configuration and OPC technology are used to establish the data communication between each station and the production line server. The program of the production line server is designed in combination with the database interface to process and save the production data in real time. In the aspect of active control, PLC process control program is designed, database query function of production line server is cooperated, man-machine interaction of touch screen is realized, and active control of local production is realized. Finally, since the MES system of E _ 2 pipe string custom assembly line was put on line for half a year, through the statistical analysis of the actual production data, the execution time of the MES system of the whole production line is about 7.7 seconds. The waste rate of the production line is less than 2.4, which is about 20% lower than that before the implementation of the system, which indicates that the design system is effective in quality control. The automatic control of process flow simplifies the work of personnel management, material statistics and product inspection, and meets the requirements of MES for real-time, integration and automation of the system. The scheme of data acquisition and active control system based on MES proposed in this paper plays an important role in reducing the operation cost, improving the overall efficiency and ensuring the product quality. The scheme has strong practicability, good promotion value and broad market prospect, and provides a good example for the further development of MES.
【學(xué)位授予單位】:上海交通大學(xué)
【學(xué)位級別】:碩士
【學(xué)位授予年份】:2012
【分類號】:TH165
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