合成革生產(chǎn)線自動涂臺系統(tǒng)設(shè)計
[Abstract]:With the rapid development of synthetic leather industry in recent years, China has become the world's largest consumer of synthetic leather, a large country of production and import and export trade. In the stage of synthetic leather production, it mainly depends on manual control of lifting knife and sizing of synthetic leather paste. Not only the intensity of labor, but also the toxic gas emitted by slurry will seriously endanger human health and cause environmental pollution. Based on the deep analysis of the operation technology and mechanism of the existing coating platform, a set of automatic coating platform system for synthetic leather production line is designed in this paper, which can conveniently transform the existing coating platform and complete the automatic operation of the coating platform. In order to achieve the full automation of the painting process, seal production, effectively solve the environmental pollution problem. The main contents of this thesis are as follows: (1) the system structure principle and operation flow of the old painting platform are designed and analyzed, and the shortcomings of the current system are pointed out. Thus, the overall design scheme of automatic painting platform system is put forward, which is divided into two subsystems: automatic lifting tool system and automatic sizing system. The two systems are described respectively. (2) the automatic tool lifting system is designed and analyzed the basic principle of joint detection based on visual image and the overall scheme of lifting tool control system based on visual detection is designed. Based on the analysis of the field technology and mechanical transmission structure of the coating platform, the solution of the speed detection of the release paper is studied, and the principle and algorithm of the coordinated control of the parameters such as the visual image sensor, the speed of the release paper, the time and the position of the lifting cutter are studied. Finally, a set of automatic lifting tool control system is designed, which is compatible with manual control system. The hardware design and software algorithm program of the system are completed. The accurate control of the position of the lifting cutter is realized. (3) the design of the automatic sizing system is first put forward with the analysis of the functional requirements of the system. Then the mechanical structure and electrical control module of the system are analyzed and designed in detail. The mechanical structure of the system includes the design of sizing mechanism and scraping mechanism. The electrical control part of the system includes data acquisition module, output control module and controller design. In view of the limitation of PID control algorithm, this paper puts forward the control algorithm of feed tank liquid level, which is mainly based on sequential control method. Thus the stable control of the liquid level in the feed tank is realized. (4) the system designed and developed in this paper is installed and tested in a synthetic leather production enterprise in Lishui. The test results show that the joint detection effect of the lifting system is good, the recognition rate can be up to 100, the lifting and dropping of the knife can be controlled accurately, and the height of the liquid level of the feed slot in the sizing system can be maintained in a stable state for a long time. The system has the advantages of stable performance, strong practicability, simple operation and good sealing performance.
【學(xué)位授予單位】:杭州電子科技大學(xué)
【學(xué)位級別】:碩士
【學(xué)位授予年份】:2016
【分類號】:TP278
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