CNG母站脫硫脫水設(shè)備工藝優(yōu)化研究
發(fā)布時(shí)間:2018-03-08 12:23
本文選題:壓縮天然氣 切入點(diǎn):脫硫脫水 出處:《東北石油大學(xué)》2015年碩士論文 論文類型:學(xué)位論文
【摘要】:壓縮天然氣(CNG)氣質(zhì)對(duì)我國(guó)天然氣產(chǎn)業(yè)發(fā)展具有重要意義,目前我國(guó)天然氣質(zhì)量標(biāo)準(zhǔn)同國(guó)外標(biāo)準(zhǔn)相比仍有一定差距。大慶地區(qū)處于我國(guó)東北部,因多種原因,壓縮天然氣氣質(zhì)更低于全國(guó)平均標(biāo)準(zhǔn),其脫硫脫水水平已然成為制約行業(yè)發(fā)展的重要因素。CNG加氣母站脫硫脫水工藝及脫水指標(biāo)是否合格直接影響整個(gè)燃?xì)馄髽I(yè)能否平穩(wěn)運(yùn)行。一是脫硫指標(biāo)不合格不僅對(duì)輸運(yùn)管路、設(shè)備及加氣車輛燃油動(dòng)力系統(tǒng)造成腐蝕,而且影響后續(xù)加工(如導(dǎo)致催化劑中毒),為設(shè)備設(shè)施的平穩(wěn)運(yùn)行埋下嚴(yán)重安全隱患,甚至威脅人身安全;二是北方地區(qū)冬季寒冷漫長(zhǎng),如果脫水指標(biāo)不合格,設(shè)備必然出現(xiàn)凍堵情況,嚴(yán)重影響母子站安全運(yùn)行和居民平穩(wěn)供氣。本文以大慶中石油昆侖燃?xì)庥邢薰炯t崗母站為研究對(duì)象,重點(diǎn)開展脫硫脫水設(shè)備工藝優(yōu)化研究,對(duì)設(shè)備改造、分子篩選型、填料配比及參數(shù)調(diào)整等方面進(jìn)行優(yōu)化,最終獲得東北高寒地區(qū)設(shè)備運(yùn)行參數(shù)最佳配置,確保設(shè)備平穩(wěn)高效運(yùn)行。通過(guò)以上研究可以獲得加氣站脫硫脫水系統(tǒng)性能及設(shè)備優(yōu)化選型的理論支撐,為加氣站設(shè)計(jì)、建設(shè)和運(yùn)行管理提供科學(xué)依據(jù)和實(shí)際參考。
[Abstract]:The quality of compressed natural gas (CNG) is of great significance to the development of natural gas industry in China, and there is still a certain gap between the quality standards of natural gas in our country and that of foreign countries. The quality of compressed natural gas is even lower than the national average. The level of desulphurization and dehydration has become an important factor restricting the development of the industry. Whether the desulfurization and dehydration process and dehydration index of CNG filling master station are qualified or not directly affects the smooth operation of the whole gas enterprise. Equipment and fuel power systems of aerated vehicles cause corrosion, and affect subsequent processing (such as poisoning of catalysts, serious safety risks for the smooth operation of equipment and facilities, and even threats to personal safety; second, long cold winters in northern areas, If the dehydration index is not up to standard, the equipment will inevitably be frozen and blocked, which will seriously affect the safe operation of the mother-child station and the stable gas supply to the residents. This paper takes Honggang Mother Station of Daqing PetroChina Kunlun Gas Co., Ltd as the research object. The process optimization of desulphurization and dehydration equipment was carried out, and the equipment modification, molecular sieve selection, filler ratio and parameter adjustment were optimized. Finally, the optimal configuration of equipment operation parameters was obtained in the northeast alpine region. Through the above research, the theoretical support for the performance of desulfurization and dehydration system and the optimal selection of equipment can be obtained, which can provide scientific basis and practical reference for the design, construction and operation management of the gas filling station.
【學(xué)位授予單位】:東北石油大學(xué)
【學(xué)位級(jí)別】:碩士
【學(xué)位授予年份】:2015
【分類號(hào)】:TE96
【參考文獻(xiàn)】
相關(guān)期刊論文 前1條
1 趙琴;;CNG加氣站分子篩脫水裝置的設(shè)計(jì)計(jì)算[J];廣東化工;2014年10期
,本文編號(hào):1583885
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